In summing up the progress on the 48xx before it went into storage, I mentioned that there was some damage to deal with. Although the locomotive, and all the associated parts, had been kept in its own box and then packed in a crate, it had still been bounced around, transported halfway across the country, etc, etc.
Fortunately, when I finally was able to take the parts back out and inspect them, the damage that had occurred was minor. All that had happened was that one of the pipe fittings on the rear buffer beam had broken free:
48xx pipe repair (1).JPG
This (and the others on both front and rear bufferbeams) had previously been glued in place. I used Slo-Zap superglue, which I like for sticking these sorts of components. It gives you time to adjust the position of what you are sticking, you can place it carefully with the end of a cocktail stick, and it can be used to build up fillets of glue to strengthen the bond. Unfortunately, like all superglues, it is brittle, and vulnerable to knocks. I suspect that is what has happened here. It's not the first time that I've knocked one of these pipes off.
This is the prototype part, and how it is mounted. The picture was taken during the setting up of the preserved 48xx at the Warley Show a few years ago. You will see that the mounting plate has very little overlap with the bufferbeam. This is what I aimed to replicate in attaching it, and what proved to be the point of weakness.
48xx pipe detail.JPG
This is the lost-wax cast part. There are a couple of lumps that replicate the fixing bolts to the bufferbeam.
48xx pipe repair (2).JPG
I decided that the strongest form of repair that I could do would be to replace the cosmetic fixings with real ones, pinning the pipe onto the bufferbeam.
The first step needed to be to file away the bolt heads. There was no way that I (or my eyesight!) could centre a drill on the top of the cast bolt,
and have the drill bit stay in place on a slightly domed surface. So I popped it into the vice, and ran a needle file across it a few times.
48xx pipe repair (3).JPG
Having prepared the surface, this is how I drilled it. My trusty Proxxon TBM220, with a 0.6mm drill in the chuck, drilling into an offcut of oak bookshelf. Without the Proxxon, I wouldn't have stood a chance of doing this accurately, by hand, using a pinchuck. And it would have taken an age, given the hardness of lost wax castings.
48xx pipe repair (5).JPG
And this is the result. Two neat holes drilled through, in roughly the right places. I didn't break the drill bit either
48xx pipe repair (4).JPG
The next thing to two was to drill matching holes in the bufferbeam. This is one of those jobs that needs about four hands, to hold the model, the casting, and then wield the drill. Not being excessively endowed in the limb department (although I do have above the average number) I used the vice again. The locomotive body is clamped gently in. Being made of plastic, I was aware of the risk of marking it. So the blue rag in the background is actually by usual workbench rag (a life-expired cotton handkerchief) protecting the parts of the body within the vice jaws.
48xx pipe repair (6).JPG
I had also previously used a new and sharp scalpel blade to remove the remaining traces of glue from the bufferbeam, and generally smooth the surface ready for the casting. It looks a mess in the picture (not helped by the previous paint-stripping incident here
https://www.scalefour.org/forum/viewtopic.php?f=90&t=6987&start=75#p77218) but isn't that bad. The surface is sufficiently smoothed. Here are the two mounting holes, drilled through the casting as a guide.
48xx pipe repair (7).JPG
The pins/bolts/pegs themselves were made out of straight brass wire. I get through packs and packs of this stuff. Having properly straight materials in a variety of sizes makes life so much easier when it comes to making parts, adding detail, cleaning out the nozzle of the superglue bottle, etc...
48xx pipe repair (8).JPG
The casting went back into the vice (yes, I do clean it from time to time to get rid of the flux splashes) and I then had the tickly job of soldering the two separate lengths of wire in place. The first one went in fine, nicely square and clean.
At the first attempt to solder the second wire in alongside it, it all went horribly wrong. Despite using the smallest touch of solder, the flux caused it to leap across the gap between the wires, and make the whole thing a single wire and solder lump
So I had to unsolder both wires, clean up the casting, and try again. This time, I used black permanent marker on the "tails" of the wires, to ensure that the solder didn't flow on to them. It worked successfully, and this was the result:
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